So, after all of the hastle with the ECU Master Det3 piggyback, I decided to opt for the MS3x. I hadn't spared any expenses up to this point so why start now?
Here's a picture of the MS3x installed in the glovebox (a clean job if I do say so myself) along with a picture of my LSx ignition coil coversion. Mint!


So after installed the MS3x, the ignition coils, and got the autotune software, I was off to the races.... almost.
I had used the autotune software to get a road tune and dialed in my idle all on my own (insert pride and overconfidence here). During all this and what I had read on the forums, I dialed my boost into about 10-11lbs and started to play with timing. That's when things got funky. I was having an absolutle blast tuning the car and pulling power out of my new setup. I was having weird idling issue and backfiring so i pulled my plugs to find this....NOT pretty.

After swapping the plugs out, the car felt even better (insert more confidence here) and was pulling like a madman. I was breaking traction in 3rd with my 4.10 LSD. Time to upgrade that too. So I did what anyone else having traction issues would have done. I aired out the tires to 25psi and threw 50 extra pounds of cement in the trunk. The car hooked, felt amazing, pulled like all hell, and sounded even better. We even did this to a cheep-o intercooler coupler a few times.

I was more concerned with keeping boost down not to pop the headgasket when I should've been more conservative with timing...
The car started to burn some oil and lost power so I decided to run a compression test because replacing the HG was inevitable right? Well here's the results...uh oh

It was definitley time to pull apart this motor. I was actually kind of excited to get the experience and dive deeper into the build. Here's some pics of the teardown and something that made my heart drop when the head came off. The pieces of metal next to the penny were found when draining the oil pan.





So I melted the piston head. Oh well. Currently I'm at school away from home and that's how she sits in the garage. When i come home for thanksgiving break I am going to pick up a used block and get an MLS gasket and ARPs for the holidays. I'm hoping to have the car back together and tuned by mid-January if the weather allows me to get to a tuner for the weekend. I'm definitley bummed it's not just the headgasket, but I plan to clean up the engine bay a bunch, and replace some clutch components when I pull everything anyways. Also, I have another surprise coming within the next few days so stay tuned! Sorry it took so long to get this thread back up (thanks photobucket), I do want to document everything here though so I can look back on it.












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