AN INDIVIDUALS LACK OF ABILITY TO PROPERLY REBUILD AN ENGINE!!!

Someone must have tried to "refresh" the top end.....but didn't understand the process of using a torque wrench. The HG was fine, I'm pretty sure it was the 3 or 4 bolts in the middle of the head that weren't properly torqued.

You can see in the above photo that cylinder 4 and 5 is the area of the loose head bolts. I also found this problem (lack of proper torque) when removing the exhaust manifolds. On the plus side it looks like someone forked out money to have this head redone, or its a reman.

Super clean, no wear at all of the valve train for a motor with 176k, and the valve guilds look brand new.


I'll be pulling the lower end and tranny this weekend. Look for a sale thread, I'm going a different direction with the car.
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