





Sorry for potato pics.
Well it wasn't without incident... As I was downshifting into 3rd there was a popping noise and then I couldn't get it into second.. So I pulled into a neighborhood and try to figure out what was wrong.. Smoke was pouring out from under the car, smoking from the O2 bung area (not sure why, I think they were unrelated) but then it decided it was gonna work and then I had no shifter problems...
From there, it was ok till towards the end... The car got really hot, when I was sitting at the light, smoke was pouring out from under it.... This is due to the 4.10LSD, which meant at 80mpg my eta was spinning at 4k, causing it to get really hot. When I got home I checked the coolant reservoir and it was almost empty.


















:hitler:
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