Finally, I have actual progress to report. First off, the CPS + DME got it running, but not good. Since the stomp test actually works now, I performed it and got a 1215 (MAF). Popped the intake off to find a mess of dryrotten vac lines, along with one of the ICV hoses completely severed. That would explain basically all of the problems. So, while waiting for the hoses, I started preparing to remove the M10


During the removal process

Currently, it is ready to be removed. If it hadn't rained (which preventing me from rolling the donor car outside, as the M50B25 is currently sans intake) I would already have it out. So, tomorrow's goal is to remove the motor, clean the bay, and begin prepping the e30 to accept its new 24v powerplant.


During the removal process

Currently, it is ready to be removed. If it hadn't rained (which preventing me from rolling the donor car outside, as the M50B25 is currently sans intake) I would already have it out. So, tomorrow's goal is to remove the motor, clean the bay, and begin prepping the e30 to accept its new 24v powerplant.
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