KI4UJO's 24v Build and M42 DD

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  • KI4UJO
    replied
    Being in the south, its mandatory. I ran two summers without it, and I'm not doing that again.

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  • E30NJ
    replied
    I like how you are keeping the A/C. Nice work! Keep it up.

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  • Codym42
    replied
    Nice!

    Interested to see how the sub box turns out. I'm hoping to make one soon too. I'm planning on doing that with a Rockford Fosgate DVC 8" and that same amp.

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  • KI4UJO
    replied
    Time for the details - finally.
    I intended to have the car finished by the beginning of August. While I could drive the car under its own power on July 31, it had no exhaust and leaked coolant. After fixing the leak and installing an exhaust, it re-entered DD duty.

    However, as with any major project, it had its problems. I had to remove the in-tank fuel pump three times (Walboro 255) due to problems with the rubber flex line which connects the pump to the steel hard line. Also, I learned to hate my loud exhaust and am now running a temporary setup to quiet it down.

    Currently, it is out of commission due to my non-leaking e36 rack deciding to leak. I have a 40k mile e46 ZHP rack waiting to be installed next week.

    Lastly, I'm overhauling the audio system again. While the OEM system was nice, it now shows the fact that it is made of used items. The new components will be

    Kenwood Exceleon KDC-X998
    Planet Audio AC1800.5
    Lukebox (Well, my attempt at building one)\

    Ok, now I'm up to date.

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  • KI4UJO
    replied
    Ill fill in the details later, but...







    Sent from my Car Phone

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  • KI4UJO
    replied
    Photo dump time!



    Painted m50 (started swapping the pan today, not shown)



    Current condition of the bay



    e32 V8 Booster



    I decided to add cruise while the dash was out for a hvac box swap.





    I'm happy to see the extra stalk present. It should make long trips easier.

    Onto the replacement heater box



    Prefered electrical tools of this job





    e36 rack



    spacers(yes, the photo sucks)



    Since I want A/C, and decided to go r134 simply because I already have the equipment (I have 609 certification and could do r12, but then I would have to get different gauges and hoses). So, my parallel flow condenser



    Upgraded junkyard fan



    Compared to the original



    New Dryer



    Evap core has been flushed of mineral oil, along with all of the black O-rings being replaced with green HNBR Rings.

    Another item that I added last year was manual windows. I enjoy features such as A/C, but don't feel that power windows are worth the extra equipment. Besides, both motors went out within 3 days of each other.

    I finally lowered it as well.



    Lastly, the completed swap adapter (well, almost. I'll wrap it up once I verify that it works)



    That's it for now.

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  • Codym42
    replied
    Good work man! Keep it up

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  • KI4UJO
    replied
    I fixed the e36. Then, I did with it what e36's were intended to do - donate their drivetrain to an e30.









    Buying this was well worth it. Degreasing this and the bay were much easier tasks.



    My clean m50, brought to you by Super Clean - the prefered degreaser of KI4UJO



    The bay, after being sealed with KBS RustSeal. I'll be spraying it in Delphin Metallic tomorrow (whole car is going back delphin eventually)





    At least the e36 enjoyed its last drive



    Nov. 1991 to July 2014 - May it rest in pieces (it doesn't have much an option)







    Other parts which are going into the e30

    e36 rack (m50 had an oil leak)



    The other e21 recaro



    Various other stuff



    Bay gets sprayed tomorrow, m50 getting dropped in next week.

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  • KI4UJO
    replied
    The M10 is out.



    Fortunately, I have a good e36 rack to replace this



    With no motor, my e30 now reminds me of an altered wheelbase drag car.





    Lastly, the boat anchor. It served me well. For my dad, it served as a powerplant for his DD'ing uses form 1994-2000. I put it back into service in 2010. I'm not sure what it's future holds. Whatever it is, it will require a trip to the machine shop.

    Last edited by KI4UJO; 06-22-2014, 08:15 PM.

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  • KI4UJO
    replied
    Finally, I have actual progress to report. First off, the CPS + DME got it running, but not good. Since the stomp test actually works now, I performed it and got a 1215 (MAF). Popped the intake off to find a mess of dryrotten vac lines, along with one of the ICV hoses completely severed. That would explain basically all of the problems. So, while waiting for the hoses, I started preparing to remove the M10





    During the removal process



    Currently, it is ready to be removed. If it hadn't rained (which preventing me from rolling the donor car outside, as the M50B25 is currently sans intake) I would already have it out. So, tomorrow's goal is to remove the motor, clean the bay, and begin prepping the e30 to accept its new 24v powerplant.

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  • KI4UJO
    replied







    Sorry for the somewhat bad phone photos. Anyway, that's the "bad" side.

    Back to e30 world, my donor car quit running. It has a bad CPS, along with weird DME stomp test results. DME and CPS will be here Wednesday. Provided that goes well, the motor could come out this week.

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  • Codym42
    replied
    That sucks. I hate seeing stuff like that. Glad you're alright

    Sent from my XT1058 using Tapatalk

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  • Coyote_ar
    replied
    damn, thats really sad. at least you and your dad are ok.

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  • KI4UJO
    replied
    Power Tour didn't go so well. Me and my dad started this morning with this :



    I'm the guy in the reds shirt.

    This happened on I-85, 30 miles from the final destination of zMax dragway:


    We got clipped while trying to merge (by a driver that just drove away, I might add) and spun backwards into the cincrete embankment at around 60 (MPH for you EU guys). It it totaled. It now has a warped frame, doors that are unable to open, and a completely demolished rear clip. Anyway, we walked away shaken but uninjured. Needless to say, the lord was watching out for us today.

    For reference, this was last month:


    This was left by the rear end:



    Ill get better photos tomorrow or monday. I'm just glad we're not dead. We almost got T-Boned by a Tahoe.

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  • KI4UJO
    replied
    Originally posted by Nick_S
    What rear end are you using for the swap?
    I'm not sure yet, but the stock early 318i 3.64:1 will have to go. On another note, I bought these today at the PnP yard



    Yes, they're racelands. However, for what I paid for them, I can't really go wrong. I'll mount them this week and give an honest review, as I will be coming from recently refreshed stock suspension.

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