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Lira (euro DS mtech II 318is reshelled, 24v swapped, also now BAR'd)

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    #61
    whoa! that is a serious e30 and a legitimate 320is!
    cars beep boop

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      #62
      i wish the underside of my e30 looked like that....friggin northeast winters
      1991 318is ---230K - DD
      1991 318i ---- 308K - retired

      Originally posted by RickSloan
      so if you didnt get it like that did you glue fuzzy oil to the entire thing?

      Comment


        #63
        a pressure washer'll do that for ya ;)

        also, something is wrong with my M50. This is copy pasted from my thread in the 24v subforum in the hopes that maybe someone will see it.


        the symptoms

        once car is hot, idling for less than a minute will lead to it violently stumbling once, throwing the 1221 O2 sensor code and having a rougher idle thereafter.

        No code is thrown during driving.

        Power feels normal until code is thrown, there is no misfire or hesitation.

        The idle is normal until code is thrown.


        things I've tried with no effect

        replaced oxygen sensor with a new one

        replaced MAF with a different used one

        replaced ICV with a cleaned, working one

        replaced injectors with known-good ones

        replaced coils with known-good ones

        replaced spark plugs with new ones

        replaced fuel filter with a new one

        replaced TPS with a known good one

        checked manifold vacuum; -20inhg (in spec)

        leakdown test; 0% 0% 3% 1% 0% 0%

        smoke test; no leaks

        reset ECU; no change

        replaced ECU with stock-tune 413; no change


        remaining diagnostics

        meter out the TPS

        meter out the MAF

        monitor fuel line pressure
        cars beep boop

        Comment


          #64
          update: 3.2 bar / 46PSI in the rail with the car on.
          cars beep boop

          Comment


            #65
            Sounds like your issue is when it goes into closed loop. 3.2 bar is a little low for the M50tu. It should be closer to 3.5bar, doesn't sound like much but the slightest fuel pressure drop when in closed loop can cause a lean misfire. Are you still using the M42 fuel pump? Once the code is thrown and the idle becomes rough, how does it run under a load/higher RPM? could have something to do with EGR if you still have it, or CCV, PCV?

            I may be wrong but its something to consider. just my .02 cents.


            awesome build BTW . I wish I could get some headway on my E30 (11 years in the making project).
            Last edited by TrixE30; 10-27-2015, 09:17 PM.

            Comment


              #66
              In!


              Dustin Wark | Instagram tumblrFlickr

              Comment


                #67
                Originally posted by Javier h View Post
                I saw this on craigs and thought of your car somewhat. An Mtech2 with an M3 engine.





                Crack pipe

                Originally posted by TrixE30 View Post
                Sounds like your issue is when it goes into closed loop. 3.2 bar is a little low for the M50tu. It should be closer to 3.5bar, doesn't sound like much but the slightest fuel pressure drop when in closed loop can cause a lean misfire. Are you still using the M42 fuel pump? Once the code is thrown and the idle becomes rough, how does it run under a load/higher RPM? could have something to do with EGR if you still have it, or CCV, PCV?

                I may be wrong but its something to consider. just my .02 cents.


                awesome build BTW . I wish I could get some headway on my E30 (11 years in the making project).
                3.2 bar is high for idle. it should be 43psi at idle IIRC. 3psi will make almost no difference though. The problem is eslewhere

                51psi should be with the vacuum line of the FPR unplugged.

                it's definitely triggered by something that runs in closed loop if the car runs well before operating temp

                Comment


                  #68
                  the weird thing is it's fine at operating temp as long as i'm driving it. it's the idling that pops the CEL.
                  cars beep boop

                  Comment


                    #69
                    also I guess I missed an update cause i've been busy with the darn CEL

                    the car is back from the exhaust shop and, well, good news and bad news on that front

                    the following things happened
                    - the front flanges and x pipe got cut off a stock e36 325is downpipe
                    - pipes were run from the flanges placing the x-pipe in a stockish location
                    - two Walker 80801 CA cats were welded in post-x-pipe
                    - a stock e36 M3 muffler had its nice pipes and flanges cut off and new pipe run directly to the cats

                    good news is that it was all run really high up and form-fitting to the body, so I have a ton of clearance



                    bad news is it's a bit of a hatchet job. the work is well done, but not really.. right.







                    the ehxaust tips will be extended, waiting for them to be delivered

                    eventually (when I do the suspension), I'm taking the exhaust down, grinding down the welds and welding in a flange post-cat so that I don't need to take the whole thing out in one giant-ass piece every time I want to fiddle with stuff behind it.

                    the plan was to BAR it and then do the suspension refresh and sideskirt repair, but my new appointment isn't for a while.


                    Originally posted by TrixE30 View Post
                    Sounds like your issue is when it goes into closed loop. 3.2 bar is a little low for the M50tu. It should be closer to 3.5bar, doesn't sound like much but the slightest fuel pressure drop when in closed loop can cause a lean misfire. Are you still using the M42 fuel pump? Once the code is thrown and the idle becomes rough, how does it run under a load/higher RPM? could have something to do with EGR if you still have it, or CCV, PCV?

                    I may be wrong but its something to consider. just my .02 cents.


                    awesome build BTW . I wish I could get some headway on my E30 (11 years in the making project).
                    thanks! and get to work!


                    I think it runs fine in closed-loop until it has to sit around and idle while hot. it'll run for a while when cold, as well, just eventually hits some amount of cold idle and trips over its own shoelaces

                    I'm still using the m42 pump, yup. I haven't volume tested it but car doesn't seem to have a miss at WOT at all.

                    I haven't run it with the CEL on, that test is scheduled for tomorrow.

                    the CCV/PCV is new and seems to be functioning normally. the purge valve is present and hooked up as well, but I haven't tested it for function yet.


                    also I've been giving it the beans while testing, and the M50 has a totally pleasant amount of power. I see why you people do this now :evil:
                    Last edited by kronus; 10-28-2015, 12:18 AM.
                    cars beep boop

                    Comment


                      #70
                      I've metered out the TPS, CPS, CTS, ATS, MAF and O2 sensor and everything is nominal. still chasing this stupid thing.

                      edit:

                      CPS: 528 ohms

                      TPS: 1450 ohms to 4790 ohms, full sweep is fine

                      ATS: 2340 ohms at ambient temp

                      CTS: 1990 ohms at ambient temp

                      MAF: .8V at idle, ground ok

                      O2: 2500 ohms heater resistance, continuity to DME ok

                      beating my head on it: yes
                      Last edited by kronus; 10-30-2015, 11:49 AM.
                      cars beep boop

                      Comment


                        #71
                        went to a shop with an autologic unit; either there's a O2 sensor wiring fault, or both MAFs I've been testing with are bad. Car wants to run lean.


                        also got the sides done. first, template



                        then drill (I started with a 3/8" bit and then used a step bit to enlarge to 5/8")



                        then mount



                        then get the pods on





                        then drive out into the daylight and admire



                        I also got the 80/88 fan switch in, but it's not engaging the low speed, so my fan resistor is likely trashed.

                        cars beep boop

                        Comment


                          #72
                          I doubt it's the MAF, it worked when I pulled it and it was stored indoors. Also cleaned the piss out of the element.

                          They typically only go bad when there's oil deposits from a filter on the element.


                          Sent from my iPhone using Tapatalk

                          Comment


                            #73
                            yeah, I tried three other MAFs with the exact same behavior.

                            yesterday I swapped the harness to an unmodified E36 M50 one. tomorrow I am putting together an X20-C101 adapter and will see if it's any different. if it works fine, I'll repack it in to the M42 housing.. I have some hope.
                            cars beep boop

                            Comment


                              #74
                              is your car loosing the 5v reference when it starts acting up?
                              Build Threads:
                              Pamela/Bella/Betty/325ix/5-Lug Seta/S60R/Miata ITB/Miata Turbo/Miata VVT/951/325xi-6

                              Comment


                                #75
                                dunno! where can I check that

                                also finished up swapping in harness that came from a known good car. same symptom.

                                swapping cam/crank sensors, and if that doesn't work I'm going to start sacrificing small animals.
                                cars beep boop

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