I recently purchased an 86 325e for my son to drive (first car) and have been working through some issues to make it reliable for him. I knew there were issues with the cluster when I bought it, no worries, anything can be fixed. It's a lot better than it was but still not as good as I'd like.
The main issue and my biggest concern was the fuel and more importantly the temp gauges. I've managed to get the temp gauge rock solid and the fuel working and correct about 90% of the time. The fix for these was a combination of cleaning and adding some solder to the grounding points on the board and making sure they were tight when I put everything back together.
The one that's driving me nuts is the tach. Sometimes it works sometimes it doesn't. Yesterday in my latest attempt to fix them all, I reflowed all of the pins for the blue, yellow and white multipin connectors as well as about 80% of the other solder connections on the board. I did not reflow the connectors where the SI board, tach and spedo connect. I put everything back together and all gauges worked but I only had one working cluster illumination light. I thought maybe I knocked a bulb loose or perhaps it just went bad. A few hours later I went out for a test drive and both of the illumination lights worked but no tach. The econometer has always still worked even when the tack doesn't. This morning I drove the car to work and still no tach. No tach at lunch. This evening leaving for work I was back to all gauges working and only half of the dash lit. On the way home the cluster became fully lit and I still had a tach.
I believe the SI board is ok. It was replaced at some point as it's the newer style with lithium batteries and orange sealant all over it. Also I have reset the SIL and all lights have remained out as one would expect.
I have searched and read and then searched and read some more to get to this point and am running out of ideas.
I did not use flux when I reflowed the board yesterday. Could this be an issue? Maybe I should flux and try one more reflow?
Is there a crack in the board?
I have also cleaned ground connection G200.
I have removed and reseated fuses 9 and 10
I've checked the 3 pin connector C104 for tightness but not signal.
I've also removed an aftermarket stereo installation where a PO had hacked into the heat dial for illumination and the OBC for 12v constant memory.
Anyone have any ideas or thoughts?
Also thanks to all who post here. There is an amazing amount of knowledge shared here that I feel lucky to have access to.
The main issue and my biggest concern was the fuel and more importantly the temp gauges. I've managed to get the temp gauge rock solid and the fuel working and correct about 90% of the time. The fix for these was a combination of cleaning and adding some solder to the grounding points on the board and making sure they were tight when I put everything back together.
The one that's driving me nuts is the tach. Sometimes it works sometimes it doesn't. Yesterday in my latest attempt to fix them all, I reflowed all of the pins for the blue, yellow and white multipin connectors as well as about 80% of the other solder connections on the board. I did not reflow the connectors where the SI board, tach and spedo connect. I put everything back together and all gauges worked but I only had one working cluster illumination light. I thought maybe I knocked a bulb loose or perhaps it just went bad. A few hours later I went out for a test drive and both of the illumination lights worked but no tach. The econometer has always still worked even when the tack doesn't. This morning I drove the car to work and still no tach. No tach at lunch. This evening leaving for work I was back to all gauges working and only half of the dash lit. On the way home the cluster became fully lit and I still had a tach.
I believe the SI board is ok. It was replaced at some point as it's the newer style with lithium batteries and orange sealant all over it. Also I have reset the SIL and all lights have remained out as one would expect.
I have searched and read and then searched and read some more to get to this point and am running out of ideas.
I did not use flux when I reflowed the board yesterday. Could this be an issue? Maybe I should flux and try one more reflow?
Is there a crack in the board?
I have also cleaned ground connection G200.
I have removed and reseated fuses 9 and 10
I've checked the 3 pin connector C104 for tightness but not signal.
I've also removed an aftermarket stereo installation where a PO had hacked into the heat dial for illumination and the OBC for 12v constant memory.
Anyone have any ideas or thoughts?
Also thanks to all who post here. There is an amazing amount of knowledge shared here that I feel lucky to have access to.
Comment