Issue resolved: Bad LC-1, analog output was connected to the wrong harness wire, probably killed the lc-1 analog output
So I recently picked up a car that was sold as not running, and it's got an MS1/extra in it.
The guy who sold it to me let the car sit with the battery dead for almost a year I think and when he got back he thought the Lc-1 went bad, which also made the MS go bad.
Anyways, I checked all the wiring for the lc-1 and it looked good, so I plugged MS into tunerstudio, made sure the wideband calibration was the LC-1 default, and turned it on. The innovate gauge read "22.4" which is right because the car is not on, tunerstudio read this:

Not really sure what that means, because the dial says one thing and the number says 7.35?
My questions:
-Does this indicate anything is broken?
-Is there a way I can test the lc-1?
-Is there a way I should be testing the megasquirt? I don't have a stim and I'm waiting on a paycheck to order one.
Let me know what I should be looking in to! Thanks!
So I recently picked up a car that was sold as not running, and it's got an MS1/extra in it.
The guy who sold it to me let the car sit with the battery dead for almost a year I think and when he got back he thought the Lc-1 went bad, which also made the MS go bad.
Anyways, I checked all the wiring for the lc-1 and it looked good, so I plugged MS into tunerstudio, made sure the wideband calibration was the LC-1 default, and turned it on. The innovate gauge read "22.4" which is right because the car is not on, tunerstudio read this:

Not really sure what that means, because the dial says one thing and the number says 7.35?
My questions:
-Does this indicate anything is broken?
-Is there a way I can test the lc-1?
-Is there a way I should be testing the megasquirt? I don't have a stim and I'm waiting on a paycheck to order one.
Let me know what I should be looking in to! Thanks!
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