OK, so I finished installing the engine.
On my first start attempt I got nothing. I fiddled with a few things and checked all my connections again. Still nothing.
I did all the checks in the Bentley with the ECU connector. Everything checks out. Fuel pump pumps, relays click, injectors click, TPS has the right response, CPS is fine, etc.
The main relay and the fuel relay seem to be fine. The fuse link in the back is fine too.
I checked the coil. Resistance readings were a bit off. + and - check was .7 ohms where the book says it should be .5 ohms. Center and + was 5700 ohms where the book said it should be 5000. It isn't far enough off to be a dead giveaway, but I am thinking this is the problem. I worked fine before I did the rebuild though.
When I turn it over, I am not getting any fuel out of the rail at the pressure regulator. And I don't seem to be getting any spark. I am sure I did the timing right. It's pretty straight forward and easy enough to do with the engine out.
The engine was running fine when I pulled it. AFM should be good.
Any thoughts on this? I appreciate the help.
On my first start attempt I got nothing. I fiddled with a few things and checked all my connections again. Still nothing.
I did all the checks in the Bentley with the ECU connector. Everything checks out. Fuel pump pumps, relays click, injectors click, TPS has the right response, CPS is fine, etc.
The main relay and the fuel relay seem to be fine. The fuse link in the back is fine too.
I checked the coil. Resistance readings were a bit off. + and - check was .7 ohms where the book says it should be .5 ohms. Center and + was 5700 ohms where the book said it should be 5000. It isn't far enough off to be a dead giveaway, but I am thinking this is the problem. I worked fine before I did the rebuild though.
When I turn it over, I am not getting any fuel out of the rail at the pressure regulator. And I don't seem to be getting any spark. I am sure I did the timing right. It's pretty straight forward and easy enough to do with the engine out.
The engine was running fine when I pulled it. AFM should be good.
Any thoughts on this? I appreciate the help.
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