pretty low key actually.. so sorry gents I know this update is lame.
engine's been perfect, butter smooth but definitely lower on torque. looks and sounds great though.
lots of parts on hand, but I haven't pulled the trigger on M20 stroking and MT1 yet. Been working the wife's allroad, emissions, turbo boost leak and a leaky arnott air bag. so a little distracted.
here are the parts waiting for install
-- RD long tube headers
-- full MT1 body kit ready for prep and paint
-- brand new front and rear console, top front trim and weatherstrip
-- new chrome for doors and rear quarters (original chrome pitted)
-- electric top frame and new tension straps in hand. still need to get an electric top cover though. hoping to swap a new manual top for one.
-- thinking about upgraded brakes but haven't pulled the trigger on anything.
lots of little gremlins have been creeping up.
-- broke my alpina wheel key, fortunately found 2 replacements via eBay australia.
-- my 2nd rack doctor E36 rack is leaking. super ticked about that. will probably end up buying a new one this time.
-- pass rear window motor died. found a replacement on ebay and swapped the motor portion of the mechanism out (kept the original gear box). replacement motor is from an 88 and I wanted to keep the original gear housing since it was molded slightly differently and has a date stamp on it.
-- pass rear wheel bearing replaced. car was completely quite for a couple of weeks but now I have a small squeak in the rear again. will probably bite the bullet and replace the other 3 bearings. will do the rear pads too.
-- my class C power amp seems to have failed.. when I pull the center stack apart I'll probably swap out the OBC with the euro clock i bought. missing the connector though so not too keen on hacking wiring.
-- windshield washer system is wacking. not getting fluid on the windows now. headlamp washers working fine though. had to disconnect the wire I added because it was temporarily shorting the entire car out. bizarre - wire never got hot or anything, but the car would go completely dead.
-- one of the euro headlights was intermittently flaking out. no problems lately. I assume it's related to the washer wiring issue.
-- also still need to deal with the hardtop headliner.
engine's been perfect, butter smooth but definitely lower on torque. looks and sounds great though.
lots of parts on hand, but I haven't pulled the trigger on M20 stroking and MT1 yet. Been working the wife's allroad, emissions, turbo boost leak and a leaky arnott air bag. so a little distracted.
here are the parts waiting for install
-- RD long tube headers
-- full MT1 body kit ready for prep and paint
-- brand new front and rear console, top front trim and weatherstrip
-- new chrome for doors and rear quarters (original chrome pitted)
-- electric top frame and new tension straps in hand. still need to get an electric top cover though. hoping to swap a new manual top for one.
-- thinking about upgraded brakes but haven't pulled the trigger on anything.
lots of little gremlins have been creeping up.
-- broke my alpina wheel key, fortunately found 2 replacements via eBay australia.
-- my 2nd rack doctor E36 rack is leaking. super ticked about that. will probably end up buying a new one this time.
-- pass rear window motor died. found a replacement on ebay and swapped the motor portion of the mechanism out (kept the original gear box). replacement motor is from an 88 and I wanted to keep the original gear housing since it was molded slightly differently and has a date stamp on it.
-- pass rear wheel bearing replaced. car was completely quite for a couple of weeks but now I have a small squeak in the rear again. will probably bite the bullet and replace the other 3 bearings. will do the rear pads too.
-- my class C power amp seems to have failed.. when I pull the center stack apart I'll probably swap out the OBC with the euro clock i bought. missing the connector though so not too keen on hacking wiring.
-- windshield washer system is wacking. not getting fluid on the windows now. headlamp washers working fine though. had to disconnect the wire I added because it was temporarily shorting the entire car out. bizarre - wire never got hot or anything, but the car would go completely dead.
-- one of the euro headlights was intermittently flaking out. no problems lately. I assume it's related to the washer wiring issue.
-- also still need to deal with the hardtop headliner.
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