M20B29 hesitation at WOT above 5k

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  • Kershaw
    R3V OG
    • Feb 2010
    • 11822

    #31
    Originally posted by apostate
    Check the Vibration damper. With the years it gets soft and in higher RPMs may "confuse" the CPS.
    Sorry that I intruded.
    I have seen this before.

    I thought I had mentioned it before, but I went back saw that I didn't. Definitely try swapping in another vibration damper.
    AWD > RWD

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    • sert57
      Advanced Member
      • May 2014
      • 170

      #32
      I ended up getting a decent deal on a DIYPNP unit, and now that it soldered together and set up, I can confirm that megasquirt did fix the problem. going to take it to a real tuner here in the coming days and get a dyno tune done.

      It sounds glorious at 7K.

      Happy the car runs right. Wish we could've figured out the issue with the motronic system but alas.

      I'm still suspicious of the vibe damper. could have been the issue.

      I'm also suspicious that the AFM isn't completely ignored in these operating conditions. I haven't seen any official documents, but it seems to be the general consensus.

      Comment

      • 2mAn
        SeƱior Mod
        • Aug 2010
        • 20119

        #33
        you should update your cars thread. I like it. Cant wait to see what this does when its fully tuned
        Simon
        Current Cars:
        -1966 Lotus Elan
        -1986 German Car
        -2006 Volkswagen Jetta TDI

        Make R3V Great Again -2020

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        • Kershaw
          R3V OG
          • Feb 2010
          • 11822

          #34
          Glad it worked out. Don't worry about the AFM or the vibration damper, they were most likely not the issue.

          Megasquirt is just the fix for this hiccup.
          AWD > RWD

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          • sert57
            Advanced Member
            • May 2014
            • 170

            #35
            I mean I agree, I'm not gonna worry about them any more, but - there SHOULD - have been a simple way to fix the issue...... especially since it has happened on others mostly stock cars.

            The engineer in me is frustrated lol

            gonna update the other threads soon.

            Thanks again for all the help guys. Really appreciate it.

            Comment

            • Kershaw
              R3V OG
              • Feb 2010
              • 11822

              #36
              I think the OEM fix is a brand new engine harness. After 30 years the shielding doesn't protect enough and something about the harmonics of the chassis and a bunch of other electrical engineering stuff that I don't understand come into play.

              A brand new engine harness was over $800 3 years ago, no idea what it is now. So yeah, Megasquirt is the answer.
              AWD > RWD

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