Checked the AFM and everything seems alright. Started at 0.25V and was smooth all the way to ~4.9V. I made sure the 2-3V range was smooth, but the issue still persists. I might have to take it to a shop so they can do a smoke test since I'm not able to find a vacuum leak. I have a new o2 sensor I can throw in to see if that helps at all
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Idle Surging (possible lean issue?)
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Glad you got it worked out, and that it was something relatively simple.
And I feel you on the knuckle-banging. Sometimes no matter how much you try to prepare for and prevent the hand from going flying when a fastener breaks loose, it still goes flying right into the pointiest, most painful thing nearby. Every damn time.
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