2nd e30, 87 Lachssilber Revival
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Engine update... turns out the breakup in the dyno graph was caused by the CPS being too far away. Stock spec does not cut it, I moved it closer and the car revs powerfully up to 7300!!!!! Unsure if I would still need larger injectors but this change with the CPS made a huge difference and the car is even that much more wild to drive.
Drove 6 hours to Lake Ontario so here's a couple pics from that vacation, nothing special...
Three people and 4 days worth of stuff, no problem.




Random Merc in the middle of nowhere gravel road
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^I liked it enough to be going back lol. Already thinking about getting dedicated autocross wheels and tires for next year.Leave a comment:
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Been doing alittle. Daily driving and cruising, trying to take pictures. I hit up a junkyard I hadn't been to in a long time and was able to find a nice rear bumper so I grabbed that to put on. Another Autocross with the CCA this weekend, should be a good time. Theres also a cars and coffee going along with it so hopefully I can walk around that if I get some down time.
Lighthouse2 by Nick Reichart, on Flickr
Hood2 by Nick Reichart, on Flickr
Side View by Nick Reichart, on Flickr
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Yeah .... that endlink was setup pretty wonky. Let me know when you want to get in and fix it.Leave a comment:
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Little maintenance update...
I replaced the front brake rotors and pads with UUC slotted rotors and some ceramic pads they were running a special on. I also replaced my intake boot that I thought may have had a small crack or at least the beginning of one and I replaced the fuel filter. I want to slowly go through my fuel delivery system to aid in flow for the engine when I eventually get the larger injectors.
I have rear pads and rotors too but never got around to switching them out. I also wanted to do a valve adjustment but I'm putting that off for another day hopefully this week.
The front rotors had the locating bolt or whatever its called already stripped out on both sides. I just drilled it out because there was no way to get out. Just the head of the bolt came off so there were still a couple thread length sticking out to locate the new rotors on with. Also when digging around under the car I noticed the sway bar link lost a nut and was sliding out. Chances are the adjustable part is not adjusted right but I put a nut on it so its together and that's all that matters right now.
Parts by Nick Reichart, on Flickr
Old Rotor by Nick Reichart, on Flickr
New Rotor by Nick Reichart, on Flickr
Sway Link by Nick Reichart, on Flickr
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Thanks guys. Hopefully with some larger injectors I'll really have a decent m20 build with the numbers to back it up.Leave a comment:
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Numbers are in... only a max HP of 182. Hugely disappointed but the place was optimistic there is still a lot left in the engine. Initial run totally blew so it was nice to see an increase of something. They suggest I need bigger injectors as there wasn't enough fuel higher in the rpm range. That and my fuel filter is probably originally so that cant be helpful. Overall the car is much smoother and feels more responsive during driving.
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Looking good man! I definitely understand given your workspace. That thing will be a blast when you get the bugs worked out.Leave a comment:
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Both of these sensors had leaks at different times. Hopefully now they are correctly tightened down and won't have anymore problems coming from them.

When I bought the RHD flywheel I got one of the vTPS from them too thinking it was cheap and why not. It worked ok but the current was never stable when calibrating in megasquirt. So I had sometime the other day and picked up the "standard" vTPS from an e36 in the junkyard. Calibrates fine now with a much more stable signal. And sunroof rust.

My poor block and the carnage it has already seen. Leftover coolant leak residue. It'll wipe off, it's just a tough spot to get to. And you can see one of the portions of the block I taped off when painting thinking something would go there lol.

And my latest problem that was fixed, crank position sensor. Revving up the car had sync loss in megasquirt around 5500 rpms making the datalog look like it was hitting a limiter. Turned out the CPS was dented enough that when the pulley gear ring spun fast enough the CPS read it as a missing tooth when there shouldn't be one. Picked the better one of my black car, so now that's on the things to buy eventually. Bad one on the right.
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