While all of this was going on, Will was working hard putting the finishing touches. At this point we were content with the mechanical side so he polished her up. He took some pics too at the Golden hour



Even with it being very dark when we arrived, I could still see the shine in the paint. It was going to be hard to sleep...
Woke up at 6am, tried to get some good rest but I couldn't wait to get my day started. It was going to be a long one too.
I planned to take the scenic route down 1 but that wasn't possible and I definitely didn't want to drive I5 because it was going to be crazy hot and with no top I'd probably die, or at least want to be dead. The plan was to make a quick stop at my parents in SanJose and then take 101 instead of 5 since it was about a 20* difference.
We grabbed breakfast, and I packed up the car, fueled up and reset the trip meter.
We fit the top in the trunk and I hope to never install it on the car, its crap but I won't throw it away

Will couldn't resist showing me the old fuel filters. These had less than 100 miles each. This comes into play here soon. He also showed me how to blow out the fuel line because there's something still in the fuel tank that blocks the fuel line.


We didn't know what the shift knob was and this bottom side is more proof. Maybe now I can finally drill that cue ball and make it a shift knob too?...

Enough of that, let's hit the road. First leg of the trip was just over 100 miles. Loving it already and got plenty of thumbs up and saw some people take pics too. This car definitely gets a good response from people

Upon arriving at my parents house the engine noise felt louder and made me really nervous. What I failed to notice was that these Type2 Solex carbs have some weird issues and I guess they go from a ~750 idle to like 1500!
I was paranoid and my brother was also moving his stuff to SanDiego so I thought screw it, let's get a Trailer and save me the risk of breaking down..... buuuuut it wasn't meant to be. Not really cheap but the problem was the 1.5 hour each way we'd have to go to get the trailer. Oh well, let's do it!
Left my parents and got moving. The car started to stumble and I remembered what Will told me . Pulled over and pulled the fuel filter, blew into the line and as I was about to put the filter back on, I noticed the crud at the bottom. Makes sense as I just drove 100 miles. Luckily we bought 3 new filters from Napa, so I installed one of those. Now we're moving! This was basically me for the next 450 miles as I took the "scenic" route

I stopped in Santa Barbara to test drive a 85M10 car, it was a pile but I did get this pic

I found the car was happiest at 3500rpms and I actually got 30mpg while going around 75mph
Car hadnt been driven since '86 and in the last 2 months Will had done about 2-250 miles. Today, she did 550 and really didn't give me any problems.
This is going to be a fun one. Time to rip out the nasty 70s carpet and put some more miles on it.

The new issue that I need to figure out is the head lights. They worked on Monday, but don't work now. Its not a fuse issue either. I really hope its not the relay, they are rare and expensive.
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