Bmw e30 - Hunt for the 8sec is ON !!
				
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 1991 BMW 318i (Old Shell RIP, Now Being Re-shelled & Reborn)
 1983 Peugeot 505 STI
 1992 Volvo 240 Wagon
 2009 Toyota 4Runner SR5 Sport 4WD
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 Now there is SPEED !!
 
 Yesterday we spent 4 hours on mounting the injector sockets THAT SUCKED !!!!
 
 But today we had more speed
 
 I went by My motorguy to help him out, i changed the bushings in the rods to a much harder and better ones.
 
 
 
 
 
 
 
 We made an rigg for the injector sockets
 
 
 Johnny keept on welding up the intake
 
 
 
 
 Johnny then moved on to the turbo pipes, dident say a thing during the evening and the it was finished
 
 
 
 
 
 I did start with the wg pipes
 
 
 
 
 
 
 one of the pipes to the wg
 
 
 Then i did the downpipe
 
 
 johnny finished up the turbo pipes
 
 
 
 
 
 when Johnny was finished with the turbo pipes we took some time to admire it
 
 
 2 happy guys
 
 
 
 
 
 
 
 
 
 
 
 
 MORE TO COMEComment
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 Think some members are missing the point this car is a DAILY DRIVER.
 
 What trim turbo are you using? Sucker looks huge. The intake manifold looks a bit small is that due to fitment? Which ems? Can't wait to see her finished up!Current: 1988 M3 - Henna/Black black alcantara
 
 Guten Parts + Service ... When you care enough to only give the very best.
 
 Previous:
 '87 S50 MTech 1 325is
 '07 DTM Audi S4
 '03 VF Supercharged M3
 '03 Lexus IS300 (615rwhp/512rwtq)
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 hey
 
 The turbo is 71mm
 
 the manifold looks small but i think it will do.
 
 there wasent any more space for an bigger one :)Comment
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 I might've missed it but how much of a lag will you have? I remember having to rev my car to 4k before the t72 gtq trim turbo started to spool.Current: 1988 M3 - Henna/Black black alcantara
 
 Guten Parts + Service ... When you care enough to only give the very best.
 
 Previous:
 '87 S50 MTech 1 325is
 '07 DTM Audi S4
 '03 VF Supercharged M3
 '03 Lexus IS300 (615rwhp/512rwtq)
 Comment
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 aren't you worried about burning through the piston with the valve notches?
 
 in several conversoations with jim at metric mechanic, he talked me out of running a piston with notches because he said there was always a problem with that once you go over 12lbs of boost. not right away but in longevity terms.
 
 just wondering if you have had any similar problems running hight boost with pistons.seien Sie größer, als Sie erscheinen
 
 
 Your signature picture has been removed since it contained the Photobucket "upgrade your account" image.Comment
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 Hmm im not sure yet.. hopefully this will go before 4k but it depends on the camshaft aswell :)
 
 
 the Old pistons i had, had bigger notches and those work well for 3 years with over 30psi of boostaren't you worried about burning through the piston with the valve notches?
 
 in several conversoations with jim at metric mechanic, he talked me out of running a piston with notches because he said there was always a problem with that once you go over 12lbs of boost. not right away but in longevity terms.
 
 just wondering if you have had any similar problems running hight boost with pistons.
 
 and even when a injector clogged up just the head gasket went.
 
 
 
 Okaj post it :) fun to seeComment
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 update Time.
 
 Its been quite for som time.. and that have sucked..
 
 All of the stand still has been due to the motor guy has to much to handle on 1 person.
 But now it seems that the speed is upp again.
 
 The new bearing is sanded
 
 
 
 
 the engine block is flattened
 
 
 
 
 
 Drilling the engine block
 
 
 
 
 
 
 
 Milling for the steal thread
 
 
 
 
 
 Hening the last of the block
 
 
 
 
 
 
 
 When the head got welded it got a bit twisted
 
 
 
 
 
 
 A friend of mine wanted to try a new foil he got home.. so i voluntared :)
 
 
 
 
 
 
 
 
 
 Jocke started to lay down the foil
 
 
 A bunch of friends got over to se the final product
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 Hopefully im putting togheter the engine block tomorow and this weekend its going in.Comment
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 Wicked. can't wait to see the finished product.
							
						http://l0st0n3.mybrute.com can't wait to see the finished product.
							
						http://l0st0n3.mybrute.com
 http://l0st-0n3.mybrute.com
 Work in progress: 1991 318i m50 swap
 
 Feedback thread :up:
 
 Originally posted by slammin.e28guyI prefer having a female in the car at all times. They generally smell good, but you do have to put up with that hole in their face.Comment
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 Damn, this is one of those threads I wish I stumbled upon after the build was done, because every time I clicked another page I got a little bit sad that eventually I was going to finish the thread.
 
 Way to go man, you guys rock. Any reason for putting the throttle body a little ways away from the intake, just packaging?Comment
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 hehe nice to hear !! thx :)Damn, this is one of those threads I wish I stumbled upon after the build was done, because every time I clicked another page I got a little bit sad that eventually I was going to finish the thread.
 
 Way to go man, you guys rock. Any reason for putting the throttle body a little ways away from the intake, just packaging?
 
 the throttel body would fit closer but we thought that this might be good.. and adding some volume to the intake :)Comment

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