M42 Turbo Build (Semi Budget, keepng AC!) No 56k
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I agree... but with keeping AC in the Texas heat (today was 100+) I can't block any of the vents. The 3 that I have there I don't have to look at them all the time anyway... only when tuning really.Leave a comment:
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Only problem I have is you have to look down to see the guages
I think in the vents is best
Looks good though, get that thing to the dynoLeave a comment:
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^Yes, I had to trim the console quite a bit. I think I cut a rectangle about 4" wide by 8" long. I have extra consoles, and I like the gauges down there... so I didn't worry about ruining a console.Leave a comment:
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Yep, mdf is great to work with. Did you trim the console at all in order for the gauge wiring to fit?Leave a comment:
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1/4"... super easy to make. Just make a template out of cardboard and then transfer to the MDF. I was thinking about ordering some carbon fiber as these would be super easy to make.Leave a comment:
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Oh, damn thats great fitment for a friction fit!! Where did you pick your's up? I purchased mine of ebay and the fitment is decent but I had to drill to small holes in it to screw it to the ashtray :(Leave a comment:
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Bottom vacuum line is input from the turbo housing. Side vacuum line is the output reference for the wastegate actuator.
Thank you. It's a friction fit, I made it so it's tight. I might go back in and use some very thin and small pieces of double sided adhesive... but really it never moves so I may just leave it as is.Leave a comment:
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How'd you mount that? Looks super clean!Leave a comment:
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More updates...
1. Got the ICV circuit working finally. It idles smooth now with AC on or off. Still has some stumbling issues (with AC on) when returning to idle at low speed, but it is 100000 times better than not being able to use the AC at idle at all. With the AC off it works perfectly now.
2. Installed a Hallman Pro Rx manual boost controller. No more boost bleed/leak at all. I now have the full 10.5psi all the way to 7000 rpms. :) I can now chirp third gear pretty easily...
3. Changed my gauge setup to something a little more aesthetically pleasing. Also turned out to be more functional as well. I like this much better. See pics.
And the bad news... we couldn't get enough guys for the dyno, so I still have no idea what this thing actually puts down. Suck. I was really looking forward to that. I have rescheduled it for sometime in October/November. Hopefully more guys will want to go out there when it is cooler.



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