I picked up this 1991 318is for a track day back in October. I took a leap of faith and decided to drive it about 100 miles to the race track with zero history on the car to 'break it in'. That ended up being a problem as it began overheating. This is my saga for this car and a log for my maintenance etc.
When this car popped up on craigslist it was advertised as a '1991 318si' and was being sold with an e36 salvage title. I decided to take a look. There was no history or records on the car, just heresay what the owner told me and a broken odometer.
I only could meet the owner in the dark and he lived on an air force base so we met at the visitor center with only light from a street lamp. The major selling point of the car was the e36 5 lug suspension conversion that had already been done. The interior was also stripped out and it had a bolt in roll cage. I took it for a test drive and the car seemed to pull pretty hard. Supposedly it also had an e36 3.73 LSD upgrade done. I picked it up and these are a few things I did to the car before the track day less than a week later. It came with 4 Style 24 wheels but 2 didn't have tires so that was a bonus and I had to plan on running the 15" style 32s.
- Removed instrument cluster and replaced instrument cluster that was non-operational, replaced burnt out lights, tried to fix broken temp gauge.
- Topped off coolant
- Installed passenger side sport seat (taurusrot/torn up)
- Checked ECU and it has an aftermarket chip
- Filled it full of tools and fluid and set off for my brother's place.
That night it began overheating, eventhough I had driven about 60 miles with no problems. I pulled over and I topped it off with water. My Brother was with me and decided to loosen the bleed screw. As he did this, the screw (which was actually a bolt) shot out of the radiator and proceeded to shoot a 10 foot high water vapor spray into the air. That night we had to be somewhere so we let it cool off and left it. we came back a few hours later, topped it off with fluids, found the radiator 'bleed' bolt in the Denny's parking lot and drove it to my brothers place where we pulled it in the garage for the night and I proceeded to try to fix the coolant leak that was now apparent.
I removed the radiator and noticed the overflow tank seemed to have an adjustment so I decided to tighten the allen bolts and that fixed the leak. We reassembled and got to bed for an exciting day on the track the next day.
The next morning the car started right up and didn't have any issues so we set off for the track about 40 miles away. On the way, the car started overheating very quickly, so I pulled over. I realized I had not bled the system and it was probably low on water. As it was idling with the hood open pulled over on the side of the road, something let go and another geyser shot out of the hood, this time coming from under the intake manifold.
After inspection it was a plastic pipe with a nipple that snapped off under the intake and it was not fixable. So we had a trailer and trailered the car back to my brother's place before leaving it and we went to the track with my friend/brother. Me with no car :(. I left the car there and went back a week later with a plan to replace the plastic water pipe under the intake. After I pulled the intake apart I looked through the parts I ordered and it turned out I had forgotten to order that water pipe (doh!)... So we went to the BMW dealer first thing the next morning, picked it up and I put it back together on Halloween. The first start was great with the only mishap being the new fuel lines swapped backwards, but its stutter start seemed to disappear and I assumed it was a vacuum issue that was now fixed. We bled the system and I drove the 75 miles home with no issues.
After thinking about it for a while now, the car reminded me of the geyser at Yellowstone named Old Faithful and I realized that may be a suitable name for the car since the old m42 is still running strong.
Since that day I have fixed quite a bit.
- New plastic coolant components
- New vacuum/coolant lines for the mess under the intake
- Replaced burnt headlight lowbeam
- Installed m44 chain tensioner
- Replaced inner/outer tie rod ends on both sides to fix sketchy steering response
- Removed e36 front style 32's that were rubbing on the coilovers
- Replaced the truck lock cylinder to one that is not drilled out
- Replaced oversprayed tail lights with spares I had
- Fixed Hot Start issue with wire on firewall
- Fixed Swaybar endlink that was held to control arm with a hardware store nut/bolt
- Fixed intermittant turn signal and realized the front bumper is held on by 2 drywall screws
- Added glove box latch so it isnt held together by a zip tie
- Replaced fuse to HVAC blower and fixed that
- Installed new shifter surround rubber
- Installed z3 steering rack
- Replaced rubber steering coupler with poly IE coupler (especially important on cars with power steering delete)
- Replaced m42 radiator with correct bleed screw
- Replaced water pump - this thing was the original pump as it took me like 8 hours to get it out (in pieces)
- Mounted skid plate to front radiator support so it is not just hanging on the power steering bolts
- Checked/replaced fuses
- Not sure if this is fixed but the rear window defroster was disconnected at the power supply by the rear window so I hooked that back up
- I believe this has non m e36 front spindles/hubs brakes so I ordered some spares for the upcoming track day. Rears seem to be either e36 or z3. Coils on it are Rokkor brand
- I added a yellow stripe so the livery on it is the german flag colors
- I replaced the oil filter housing gasket and seal and got that to stop leaking oil... now for the other side...
- Changed spark plugs
- Changed valve cover gaskets and painted intake/valve cover silver
- Repaired cracked style 24 wheel and get new rubber 215/40/17 on the rears and 205/40/17 on the fronts i believe. Potenza Pole position s-04
- Ordered/Installed 5 mm spacers and bolts so the style 32 wheels dont rub on the coils anymore
- Ordered a front strur bar for it
- Sport seats installed to replace the incorrect passenger sport seat that was in the drivers spot. They are cloth and correct driver/passenger set now
- Installed cigarette lighter outlet so now I can use an adapter to charge my phone.
- Tightened nuts on the roll cage as some were loose/drilled one oblong so it would fit the screw through
- Noticed a few oil pan bolts are missing, tried to replace but it seems the threads are gone and maybe contributing to the oil leak-still have to figure this out
- Ran fuel injector cleaner through it to clean up the injectors
- Removed the ac compressor/ lines to remove weight. The system was empty anyway, but i left the ac fan on so I can still use it as an aux fan
- Replaced hood shock that blew out over the winter
- Got an alignment after the z3 rack was installed
- Replaced the spacer that was on the sport steering wheel which had allowed some play in the wheel with enlarged washers, now it is solid and I straightened the wheel
- Added throttle clip on throttle body so it isn't held together by a metal wire and now has an actual BMW clip
- Fixed interior light switch so now it works when the door opens
- Screwed rear speakers into the rear shelf to try to find the source of a rattle - still have a rattle
The car went with me to Topeka Kansas to pick up some autocross wheels and tires. I drove it almost 1000 miles in one day in just under 15 hours. It average 66.6 miles including stops and 29.8 mpg! I figured if it could last through that it would be ready for a track day and it earned its name as old faithful! Now I'm doing an autocross tomorrow and will see how it goes. track day is in less than a month and I have a power steering delete plate coming in the mail.
Here are some photos including the cam gears when i took off the valve cover. Everything looks pretty good for an engine with no history and bullet holes in the rear end!!
- I have put over 3500 miles on the car and it hasn't missed a beat, all the while getting about 30 mpg so I can't complain.
- In the mean time the mount for the passenger window broke off so i need to fix that
- It would also be wise to get another voltage regulator before this one goes bad. You know, preventative maintenance.
I will get some pictures/ video up form my autocross tomorrow! Stay Tuned.
When this car popped up on craigslist it was advertised as a '1991 318si' and was being sold with an e36 salvage title. I decided to take a look. There was no history or records on the car, just heresay what the owner told me and a broken odometer.
I only could meet the owner in the dark and he lived on an air force base so we met at the visitor center with only light from a street lamp. The major selling point of the car was the e36 5 lug suspension conversion that had already been done. The interior was also stripped out and it had a bolt in roll cage. I took it for a test drive and the car seemed to pull pretty hard. Supposedly it also had an e36 3.73 LSD upgrade done. I picked it up and these are a few things I did to the car before the track day less than a week later. It came with 4 Style 24 wheels but 2 didn't have tires so that was a bonus and I had to plan on running the 15" style 32s.
- Removed instrument cluster and replaced instrument cluster that was non-operational, replaced burnt out lights, tried to fix broken temp gauge.
- Topped off coolant
- Installed passenger side sport seat (taurusrot/torn up)
- Checked ECU and it has an aftermarket chip
- Filled it full of tools and fluid and set off for my brother's place.
That night it began overheating, eventhough I had driven about 60 miles with no problems. I pulled over and I topped it off with water. My Brother was with me and decided to loosen the bleed screw. As he did this, the screw (which was actually a bolt) shot out of the radiator and proceeded to shoot a 10 foot high water vapor spray into the air. That night we had to be somewhere so we let it cool off and left it. we came back a few hours later, topped it off with fluids, found the radiator 'bleed' bolt in the Denny's parking lot and drove it to my brothers place where we pulled it in the garage for the night and I proceeded to try to fix the coolant leak that was now apparent.
I removed the radiator and noticed the overflow tank seemed to have an adjustment so I decided to tighten the allen bolts and that fixed the leak. We reassembled and got to bed for an exciting day on the track the next day.
The next morning the car started right up and didn't have any issues so we set off for the track about 40 miles away. On the way, the car started overheating very quickly, so I pulled over. I realized I had not bled the system and it was probably low on water. As it was idling with the hood open pulled over on the side of the road, something let go and another geyser shot out of the hood, this time coming from under the intake manifold.
After inspection it was a plastic pipe with a nipple that snapped off under the intake and it was not fixable. So we had a trailer and trailered the car back to my brother's place before leaving it and we went to the track with my friend/brother. Me with no car :(. I left the car there and went back a week later with a plan to replace the plastic water pipe under the intake. After I pulled the intake apart I looked through the parts I ordered and it turned out I had forgotten to order that water pipe (doh!)... So we went to the BMW dealer first thing the next morning, picked it up and I put it back together on Halloween. The first start was great with the only mishap being the new fuel lines swapped backwards, but its stutter start seemed to disappear and I assumed it was a vacuum issue that was now fixed. We bled the system and I drove the 75 miles home with no issues.
After thinking about it for a while now, the car reminded me of the geyser at Yellowstone named Old Faithful and I realized that may be a suitable name for the car since the old m42 is still running strong.
Since that day I have fixed quite a bit.
- New plastic coolant components
- New vacuum/coolant lines for the mess under the intake
- Replaced burnt headlight lowbeam
- Installed m44 chain tensioner
- Replaced inner/outer tie rod ends on both sides to fix sketchy steering response
- Removed e36 front style 32's that were rubbing on the coilovers
- Replaced the truck lock cylinder to one that is not drilled out
- Replaced oversprayed tail lights with spares I had
- Fixed Hot Start issue with wire on firewall
- Fixed Swaybar endlink that was held to control arm with a hardware store nut/bolt
- Fixed intermittant turn signal and realized the front bumper is held on by 2 drywall screws
- Added glove box latch so it isnt held together by a zip tie
- Replaced fuse to HVAC blower and fixed that
- Installed new shifter surround rubber
- Installed z3 steering rack
- Replaced rubber steering coupler with poly IE coupler (especially important on cars with power steering delete)
- Replaced m42 radiator with correct bleed screw
- Replaced water pump - this thing was the original pump as it took me like 8 hours to get it out (in pieces)
- Mounted skid plate to front radiator support so it is not just hanging on the power steering bolts
- Checked/replaced fuses
- Not sure if this is fixed but the rear window defroster was disconnected at the power supply by the rear window so I hooked that back up
- I believe this has non m e36 front spindles/hubs brakes so I ordered some spares for the upcoming track day. Rears seem to be either e36 or z3. Coils on it are Rokkor brand
- I added a yellow stripe so the livery on it is the german flag colors
- I replaced the oil filter housing gasket and seal and got that to stop leaking oil... now for the other side...
- Changed spark plugs
- Changed valve cover gaskets and painted intake/valve cover silver
- Repaired cracked style 24 wheel and get new rubber 215/40/17 on the rears and 205/40/17 on the fronts i believe. Potenza Pole position s-04
- Ordered/Installed 5 mm spacers and bolts so the style 32 wheels dont rub on the coils anymore
- Ordered a front strur bar for it
- Sport seats installed to replace the incorrect passenger sport seat that was in the drivers spot. They are cloth and correct driver/passenger set now
- Installed cigarette lighter outlet so now I can use an adapter to charge my phone.
- Tightened nuts on the roll cage as some were loose/drilled one oblong so it would fit the screw through
- Noticed a few oil pan bolts are missing, tried to replace but it seems the threads are gone and maybe contributing to the oil leak-still have to figure this out
- Ran fuel injector cleaner through it to clean up the injectors
- Removed the ac compressor/ lines to remove weight. The system was empty anyway, but i left the ac fan on so I can still use it as an aux fan
- Replaced hood shock that blew out over the winter
- Got an alignment after the z3 rack was installed
- Replaced the spacer that was on the sport steering wheel which had allowed some play in the wheel with enlarged washers, now it is solid and I straightened the wheel
- Added throttle clip on throttle body so it isn't held together by a metal wire and now has an actual BMW clip
- Fixed interior light switch so now it works when the door opens
- Screwed rear speakers into the rear shelf to try to find the source of a rattle - still have a rattle
The car went with me to Topeka Kansas to pick up some autocross wheels and tires. I drove it almost 1000 miles in one day in just under 15 hours. It average 66.6 miles including stops and 29.8 mpg! I figured if it could last through that it would be ready for a track day and it earned its name as old faithful! Now I'm doing an autocross tomorrow and will see how it goes. track day is in less than a month and I have a power steering delete plate coming in the mail.
Here are some photos including the cam gears when i took off the valve cover. Everything looks pretty good for an engine with no history and bullet holes in the rear end!!
- I have put over 3500 miles on the car and it hasn't missed a beat, all the while getting about 30 mpg so I can't complain.
- In the mean time the mount for the passenger window broke off so i need to fix that
- It would also be wise to get another voltage regulator before this one goes bad. You know, preventative maintenance.
I will get some pictures/ video up form my autocross tomorrow! Stay Tuned.
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