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ForcedFirebird's m20 dyno thread.

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  • digger
    replied
    50% more flow from making it a poofteenth bigger? yeah righto....they are also doing it wrong as you need a piece at the end to stop the edges of the exit being rounded over and screwing up the matching of the interface to the head

    i had a manifold treated with a similar process (but not EH) the flow numbers improved and so did the balance but it made noticeably less power by 9whp...i got a spare one treated so it wasn't the same manifold. if it made the same power then i could say maybe th operator didn't pump enough shit down its throat, but to go backward maybe the polish isn't so good? the AFR were identical within 0.2AFR the entire run with no tune changes so probably moving the same amount of air but not making power from it so combustion efficiency and BSFC down the toilet. after that i got the MM pulse tune manifold and did a cam swap
    Last edited by digger; 02-01-2019, 07:38 PM.

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  • LowR3V'in
    replied
    on that extrude vid u linked
    i don't really know what those numbers really mean but just notice
    the very even distribution of the runners.
    Seems like a good thing but based on the number differences before/after
    is it worth the money vs power you are seeing? Would it matter as much on an FI engine?
    Last edited by LowR3V'in; 02-01-2019, 06:29 PM.

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  • ForcedFirebird
    replied
    Originally posted by 2mAn View Post
    How much of a difference do you think it is with and without that 2mm off the deck? Im guessing that bumps the CR from ~8.5:1 to ~9.5:1

    The added stroke is what bumps the compression - swept volume. The 2mm off the deck is because the crank is 6mm more (3mm up, 3mm down strokes), but the rods are 5mm shorter than b25. Taking the 2mm puts the pistons back up close to the head. If you didn't shave them, you would have an extremely large quench/squish (distance between the head and pistons at TDC).

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  • 2mAn
    replied
    How much of a difference do you think it is with and without that 2mm off the deck? Im guessing that bumps the CR from ~8.5:1 to ~9.5:1

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  • ForcedFirebird
    replied
    Originally posted by LateFan View Post
    How is an "extrude hone" done in a curving intake runner like that? I'm trying to picture the hardware that does this. Is it just smoothing, or removing metal to enlarge the diameter?

    Thanks -



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  • LateFan
    replied
    How is an "extrude hone" done in a curving intake runner like that? I'm trying to picture the hardware that does this. Is it just smoothing, or removing metal to enlarge the diameter?

    Thanks -

    Leave a comment:


  • ForcedFirebird
    replied
    Originally posted by digger View Post
    my guess is the differences are mostly breathing mods
    Originally posted by LowR3V'in View Post
    looks like that cam isn't doing shit

    I just pushed the car into a spot to pull the diff, and something is dragging pretty hard. It's very easy to push backwards, but going forward is 2x the effort.



    As far as the 2 engines and the cam, one added lift/duration for more flow with nothing upstream, and the stock cam car increased flow before/after combustion. I have dyno tested headers similar to these and they are worth 5-8whp/tq - but we are missing closer to 10.
    Last edited by ForcedFirebird; 02-01-2019, 12:58 PM.

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  • LowR3V'in
    replied
    looks like that cam isn't doing shit

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  • digger
    replied
    my guess is the differences are mostly breathing mods

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  • ForcedFirebird
    replied
    Originally posted by jeffnhiscars View Post
    Could the extruded intake have made that much difference and if I may ask what that costs ?

    I have a feeling the diff is causing parasitic loss. Going to pull it out tomorrow anc check it out.


    Originally posted by digger View Post
    It's amazing that both graphs are basically identical upto 5000rpm.

    So the first has
    - standalone ecu
    - header
    - exrtrude hone
    - bbtb and fine style inlet
    - tighter squish clearance

    But the second has a IE 272, is it regrind or Schrick knock off ?

    New cam.





    Two other differences are the first one has 3.73 final drive, second has 4.10 with oil pressure relief blocked (~80ish psi oil pressure max), and first had 10w40 conventional, second had 10w60 (~65 max oil pressure) - but don't believe the oil made the difference as they both were hot enough.

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  • digger
    replied
    It's amazing that both graphs are basically identical upto 5000rpm.

    So the first has
    - standalone ecu
    - header
    - exrtrude hone
    - bbtb and fine style inlet
    - tighter squish clearance

    But the second has a IE 272, is it regrind or Schrick knock off ?

    Leave a comment:


  • jeffnhiscars
    replied
    Could the extruded intake have made that much difference and if I may ask what that costs ?

    Leave a comment:


  • ForcedFirebird
    replied
    Originally posted by redlightpete View Post
    Did these both have stock cams and non-adjustable cam gears?
    Originally posted by LowR3V'in View Post
    have you seen any power from retarding the cam seeing as allot of people resurfaced/shaved heads but with no adjustable gear.

    Honestly I have not done much with the adjustable gears on the dyno.


    Here's the graphs from Sat.



    81mm crank, 130mm rods, b25 pistons, .080" (2.03mm) off the deck, stock cam (and cam gear), in house rebuilt head, .035 quench, bored throttle body, extrude manifold, eBay headers, single 2.5" exhaust through 2 mufflers. MS1 with a smooth elbow pipe, cone filter.


    Click image for larger version

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    81mm crank, 130mm rods, b25 pistons, .080" (2.03mm) off the deck, IE 272 cam (stock cam gear), in house rebuilt head, .050" quench, stock intake/TB, stock exhaust manifolds, single 2.5" exhaust with a single resonator. Stock ECU re-mapped at the dyno.


    I believe this car "should" have made more power, was actually a little disappointed. Later after watching a video sent by a friend, I can hear a lot of diff noise that was impossible for me to hear in the car while tuning (one car bay with a dyno in it). Doubt we will bring it back to the dyno, just rebuild the diff and send it racing.



    Click image for larger version

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  • LowR3V'in
    replied
    have you seen any power from retarding the cam seeing as allot of people resurfaced/shaved heads but with no adjustable gear.

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  • Reichart12
    replied
    Ahh thanks for the clarification. I must have missed that if you mentioned it before. Still good power output.

    Leave a comment:

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