M30 swap for my Olive Drab Vert!

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  • RagtopE30
    replied
    Boosted esteem = no steam with boost

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  • jeffnhiscars
    replied
    People forget that engines have feelings too.

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  • RagtopE30
    replied
    Absolutely! I mean come on, no wonder it gave out when it has low self esteem! Painting the intake will boost it's esteem and therefore will prevent further overheating issues, or steam events!

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  • jeffnhiscars
    replied
    Originally posted by RagtopE30
    Copper spray and multiple rounds of torquing at each interval with "rest" time in between each pass. And I am going to paint my intake manifold
    I read that too...painted intake manifold is essential to a proper HG install

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  • RagtopE30
    replied
    Copper spray and multiple rounds of torquing at each interval with "rest" time in between each pass. And I am going to paint my intake manifold

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  • LJ851
    replied
    When you posted about the overheating the first thing i thought was head gasket but didn't want to say it and jinx you.

    What are you going to do differently this time ?

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  • RagtopE30
    replied
    Yes to the CS. And the blow out was the result of improper prep and install of the hg. Like I said, if Otis recommends a certain procedure for installation it is best to follow his advice.

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  • jeffnhiscars
    replied
    Is th at the CS that was at the BBQ 2 years ago and was the blow out a result of the bolts, head gasket or both ?

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  • RagtopE30
    replied
    For those of you who are following this thread for inspiration or knowledge let me put something out there. If you are lucky enough for Otis (Good&Tight) to share his knowledge with you take it as gospel truth and don't let anyone tell you different not even a hot shot machinist.

    After running the car for almost a week with the turbo installed I have noticed a "hiccup" at 12 psi at WOT. At first I thought it was my timing being slightly off but then I also had a couple of overheating situations where I lost a lot of coolant out of the overflow tank. I had to admit to myself that I had a head gasket issue. So I tore into it this evening to confirm. ONCE AGAIN, Otis's advise is the gospel truth!!!!!!!!

    You can see where the exhaust pushed through from two cylinders under the head gasket. There was only one that leaked above the head gasket.







    And the underside of the head. ONCE AGAIN OTIS IS THE TURBO M30 GOD!!!







    But it is not all bad. I had a couple of visitors today.

    First a 1972 3.0 CS came in because of a driveline vibration. A loose driveshaft slip joint nut and Guibo bolt tightened and it is back on the road.





    Then a local was out for a test drive in his newly finished project and he stopped by.





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  • LJ851
    replied
    New sig is cash.

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  • RagtopE30
    replied
    Lorin beat you to the punch

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  • Bearmw
    replied
    Can't you run a B35 auto trans TPS using three of the wires as a variable setup?

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  • RagtopE30
    replied
    I hear you!

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  • LJ851
    replied
    Originally posted by RagtopE30
    It has a different connector and I don't have one


    Thats what junkyards are for. I might have one, and i might even be able to find it. maybe.

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  • RagtopE30
    replied
    It has a different connector and I don't have one

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