So, it's pretty damn great. Sounds a little different (I don't know why, maybe I corrected an intake or exhaust leak with this rebuild), and it's definitely faster, significantly, and without the pinging that scared me last time. I gave up some compression, but maybe the headwork improved flow? I dunno, but the car pulls hard especially from 3K and up. Still on a stock chip, will swap in the MarkD chip next. Still considering going to a Megasquirt PnP management system.
So about that throttle body with the hole in it. I think I understand why it's there. I had trouble dialing in a reasonable idle. Between the lumpy cam and the lightweight aluminum flywheel, the engine was prone to stalling. So I turned the set screw that adjusted the throttle plate to get a faster idle, but then the TPS would shut off, thereby deactivating the idle control valve (ICV), so I got the romping idle. Not enough play in the TPS slotted screw holes to clock in the slightly opened throttle plate. So I think that's why someone drilled into the throttle plate. In this case, I did some grinding on the TPS mounting slots to give more adjustment, but then this prevents the switch from shutting off again at full throttle. I still haven't dialed in the fuel pressure regulator with an air-fuel meter in case the mixture is wrong and affecting idle speed. Once I do that, and if I still have a tuning problem, then I may be forced to go with the Megasquirt to compensate.
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