Brought the AC lines into work with me this morning and prepared to start calling mechanic shops to see if they could do the crimping for me. Sure enough I hit gold on the first call! Pretty sweet little mom and pop shop with an older gentleman working the desk. Brought him the lines and he looked them over. The feed line with the #10 to #12 splicer looked good and he agreed to crimp it, but he brought an issue to my attention with the #8 line. While the #8 splicer fit the e30 portion no problem, the e36 line was new and apparently an updated design with a significantly smaller OD. The ID was the same, but the OD would prevent the crimp from sealing correctly. We chatted for a bit about possible solutions and basically just decided that I'd bring the car in after I got it running and have them fabricate a line for me. So I left the feed line to be crimped and headed back to work.
While at work I did some more thinking and a bit of research and realized that aluminum brazing was a fairly regular method of fusing AC hardline, and I just so happen to have purchased some MAP gas and aluminum brazing rod a few weeks ago. At the end of the day I stopped by the shop to pick up the crimped line and discussed my idea with the guy at the counter. He provided me with a few pieces of scrap aluminum line to work with and I headed home to see what I could do.
Here you can see the issue at hand

And the pieces I'm working with



First I went into the engine bay and installed the newly crimped line... fit perfect!



Then I test fit the e36 line on the compressor and the e30 line at the condenser. One of the annoying parts was that while it would be a relatively straight shot to get them to line up, the e36 line took a dive straight down, which required you to pull a 180* and come back up to meet the e30 line. Time to make it better!

Cut the e36 line at a spot that would keep it angled up, and cut an end of the 90* #8 to #8 splicer.

Took them back to the car to test fit again and measure the distance between the two.

I used a smaller diameter flexible piece of aluminum tube I'd picked up, and added an extra 3/4" of length for my cut point. Cut it with the grinder, filed down and chamfered the outside edge.

Then took a drill bit that was slightly larger than the OD of the smaller pipe, and drilled out the e36 fitting and #8 splicer so the length of tube would fit snugly inside them.

Pressed them all together and went for another test fit. Voila!

Took a sharpie and marked the orientation and took it back to the vise for brazing.

After it cooled down I test fit it one more time and marked the orientation of the e30 soft line in the #8 splicer, and tomorrow I'll take it back into the shop to get crimped.

Honestly pretty stoked at how perfectly this worked! I'll be dropping it off at the shop again tomorrow before work and will have the entire AC system buttoned up this weekend!
While at work I did some more thinking and a bit of research and realized that aluminum brazing was a fairly regular method of fusing AC hardline, and I just so happen to have purchased some MAP gas and aluminum brazing rod a few weeks ago. At the end of the day I stopped by the shop to pick up the crimped line and discussed my idea with the guy at the counter. He provided me with a few pieces of scrap aluminum line to work with and I headed home to see what I could do.
Here you can see the issue at hand

And the pieces I'm working with



First I went into the engine bay and installed the newly crimped line... fit perfect!



Then I test fit the e36 line on the compressor and the e30 line at the condenser. One of the annoying parts was that while it would be a relatively straight shot to get them to line up, the e36 line took a dive straight down, which required you to pull a 180* and come back up to meet the e30 line. Time to make it better!

Cut the e36 line at a spot that would keep it angled up, and cut an end of the 90* #8 to #8 splicer.

Took them back to the car to test fit again and measure the distance between the two.

I used a smaller diameter flexible piece of aluminum tube I'd picked up, and added an extra 3/4" of length for my cut point. Cut it with the grinder, filed down and chamfered the outside edge.

Then took a drill bit that was slightly larger than the OD of the smaller pipe, and drilled out the e36 fitting and #8 splicer so the length of tube would fit snugly inside them.

Pressed them all together and went for another test fit. Voila!

Took a sharpie and marked the orientation and took it back to the vise for brazing.

After it cooled down I test fit it one more time and marked the orientation of the e30 soft line in the #8 splicer, and tomorrow I'll take it back into the shop to get crimped.

Honestly pretty stoked at how perfectly this worked! I'll be dropping it off at the shop again tomorrow before work and will have the entire AC system buttoned up this weekend!
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